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2fast4u88
08-08-2010, 02:17 PM
Body has 133k on it. Motor has around 4k put on it. Has a good bit of mods.
I will probably forget some but here it goes.

Engine:
102k mile b-body bottom end
Stock crank, rods and pistons. All bearings replaced by clevites.
Melling stock replacement pump with high pressure spring. Welded on moroso drag pick up tube.
Moroso 7.5 qt kicked out pan.
Cc502 with ls7 lifters
Summit moly pushrods, gm guide plates & 1.6 summit roller rockers
New valve seals/stock valve job, bullet vs574 valve springs
P&p heads and intake
Felpro 1074 head gaskets with arp head bolts
Stock tb
30lb svo's with no emissions
K&n cold air intake
Lt4 heavy duty timing set
All freeze plugs replaced, new water pump, stock thermostat(doesn't break 185), New opti, wires and plugs.
New fuel pressure regulator
New starter
All gaskets replaced. Doesn't leak or burn one drop of oil.

Exhaust:
Pacesetter race painted longtubes with new delphi o2's
Matching ory and some type of exhaust I have no clue about.

Suspension:
H&R lowering springs(1.25 drop all around)
Kyb agx's all around(less than 1500 miles)
Front strut mount mod for more travel
New outer tie rods and lower ball joints
Poly tranny mount
3pt subframe connectors
Umi bolt in relocation brackets spot welded on
Umi non adjustable lower control arms
Umi off car single adjustable phb
The umi stuff is only a few months old less that 400 miles
Ws6 wheels with new fusion tires(less than 400miles)

Body:
2 1/2 cowl hood
Conversion headlights instead of the sealed beams. I believe they use h3 or h4 bulbs.
Aftermarket fog lights
Tinted front turn signals
Tinted windows all around (I believe to be like 30%)
The bad a dent in the 1/4 right behind the driver door. Not real noticable from some angles. Was told 300 to fix it. Then the rear bumper is starting to turn the famous faded gray color.

Transmision/Rear
Stock tranny and rear as far as I know.
Stock replacement fly wheel
Stage 3 clutch kit( holds for 2nd gear drops into burnout and 3rd gear)
Pro 5.0 shifter
Tranny flush haven't got to the rear

I think that is it. There is build picture for the car/motor on here. Or I can give links which ever. Have a crap load of receipts strung everywhere.

$4000 firm or at least try to be the way it sets. With out tires/wheels (will put stock on with almost brand new tires). With out hood and rear control arms/phb. Will put all stock stuff back on $3300 firm. I will have to clean it up and snap pictures but will post some vids of it.

2fast4u88
08-08-2010, 02:18 PM
O and the way it sets it has a lc-1 wideband with a db blue gauge. But I think the sensor is on its way out or needs calibrated. Will include data cable that I picked up in jan. Though not included in the $3300 price.

Will include several tunes from solomon and myself. Along with the stock tune and everything for tunerpro on a disc. It also needs a new oil pressure sensor. As when it gets hot it likes to jump around and decided to read low. Did it since the original motor just never replaced it. As I checked it with a gauge with the new motor and was carrying 40psi at idle when the stock gauge was showing 20psi.

Here is some vids of it.


http://www.youtube.com/watch?v=8IB-eLKsAfw
This vid was on the stock tune when I first got it together. It has a new side skirt, fender, headlight cover and front bumper also.

http://www.youtube.com/watch?v=k-_WQHVSGl8

http://www.youtube.com/watch?v=Sl0rf4YU7ms

http://www.youtube.com/watch?v=p9kuVA0ZWZE
2nd gear start burnout with 1/4 throttle

http://www.youtube.com/watch?v=d8OWrpaBgso

http://www.youtube.com/watch?v=pOUPhdrpXh8

2fast4u88
08-08-2010, 02:23 PM
ehh I changed my mind. $3700 firm the way it sets cept for the hood. Will have stock hood.

2fast4u88
08-14-2010, 02:30 PM
Ok I feel like a idiot I change hoods and while I did I washed the car then sprayed the motor off. Getting something wet where it won't idle and misses at idle and part throttle. Not sure what it is cept it shouldn't be the opti. As it is sealed up tight.

Right now it sets with the stock hood, stock rear control arms, panhard bar, no wideband, has the ws6 wheels with the new tires. Wanting $2800 the way it sets. But will have to be hauled.

I will post pics when I go back to the car.

BIGT94z
08-14-2010, 06:24 PM
prolly got the opti to wet. goodluck guy

2fast4u88
08-14-2010, 10:47 PM
It isn't the opti I know that for a fact. There is no possible way water got in it. As when I built the motor everything was sealed tight. The opti is siliconed up tight. I know what is wrong with it to a point. As the icm plug rubber must have fell off having it apart at one time. And water go in it. I blew it out but is still missing not as bad though. To be honest it may have messed up the icm. Not sure though.

The not keeping idle started right before that as it has been setting for about 2 weeks with the battery off. What happened I have no idea but is setting the check engine light for it. Just never pulled the code. Really tired of messing with it and sinking more money in it. As everything you see listed was done with in 6 months. When I want to build the new turbo motor for the other one. Though hard to do looking at this one wanting more out of it. Putting the other on the back burner:hmm:

popo8
08-14-2010, 11:09 PM
.............. Wanting $2800 the way it sets. ..............I will post pics when I go back to the car.


you have gotten my attention..... where are those pics?

2fast4u88
08-15-2010, 12:58 PM
Popo whats up man? I'm going over to the body shop today and pull the wideband out. I haven't had any luck finding my charger for the camera though. I will look for it again and if I can't find it I will have to take some with the cell if they turn out ok.

Ps... I never knew your car was boosted. Sounds like a Badass ride if you would tell real numbers:)

2fast4u88
08-15-2010, 02:50 PM
Ok update it isn't missing anymore or setting the check engine light so it must have dried out. It also idles fine till it gets to temp. Once there it will idle at like 300 rpms and then die. But will stay running as long as giving gas.

Here is some pics. It rained after I washed it. Along with I haven't got time to vacuum the inside. I also have the vents to put back in. None of the seats are ripped or a stain any where inside. Also the pic of the penny in the tires is the rears. The fronts are practically perfect. Along with the right rear tailight has a little crack in it.

I also have either a sony or kenwood cd player to put in it. I just haven't stuck it back in after doing the wideband install.

http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4308.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4311.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4312.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4314.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4313.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4315.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4316.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4317.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4318.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4319.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4320.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4321.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4322.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4323.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4326.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4329.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4330.jpg
http://i110.photobucket.com/albums/n103/2fast4u88/Hard%20top%20Transam%20Rebuild/100_4331.jpg

2fast4u88
08-16-2010, 02:29 AM
Ok it is running fine now. No missing or idle problem. I guess my messing with the tb caught up to it. To the point the iac couldn't account for the air needed. Open the tb up and reset the tps. All is fine.

3k firm no wideband, stock hood, control arms and phb. The rest goes.